HOME

TheInfoList



OR:

Airborne Express Flight 827 was a functional evaluation flight (FEF) of an
ABX Air ABX Air, Inc., formerly Airborne Express, is a cargo airline headquartered at Wilmington Air Park near the City of Wilmington, Ohio, US. ABX Air operates scheduled, ad hoc charter and ACMI (Aircraft, Crew, Maintenance and Insurance) freight se ...
(under
Airborne Express Airborne Express was an express delivery company and cargo airline. Headquartered in Seattle, Washington, its hub was in Wilmington, Ohio. Airborne was founded as the Airborne Flower Traffic Association of California in 1946 to fly flowers fro ...
) Douglas DC-8-63F (registration N827AX) that had undergone a major modification. On December 22, 1996, during the test flight, the aircraft stalled and crashed, killing all six people on board. Accident investigators determined the cause of the accident was improper crew control inputs.


Background


Aircraft

The aircraft involved was a Douglas DC-8-63 freighter registered as N827AX. The aircraft had been built in 1967 and was previously owned by KLM as a passenger aircraft (with registration PH-DEB) and then Capitol Air and National Airlines (registration N929R). In January 1986 the aircraft was converted into a freighter and delivered to Emery Worldwide (with the same registration).
ABX Air ABX Air, Inc., formerly Airborne Express, is a cargo airline headquartered at Wilmington Air Park near the City of Wilmington, Ohio, US. ABX Air operates scheduled, ad hoc charter and ACMI (Aircraft, Crew, Maintenance and Insurance) freight se ...
(a subsidiary of Airborne Express at the time) purchased the aircraft on June 17, 1996, more than six months before the accident. The aircraft was re-registered as N827AX. It underwent a major overhaul and was delivered to ABX Air on December 15 the same year, just a week before the accident. The aircraft was powered by four Pratt & Whitney JT3D-7 turbofan engines. At the time of the accident, the aircraft had flown 62,800 hours and nine minutes with 24,234 take off and landing cycles.


Overhaul

The aircraft's overhaul was performed by the Triad International Maintenance Corporation (TIMCO) at Piedmont Triad International Airport in Greensboro, North Carolina. During the major overhaul, the aircraft received major avionic upgrades, including the installation of an
electronic flight instrument system In aviation, an electronic flight instrument system (EFIS) is a flight instrument display system in an aircraft cockpit that displays flight data electronically rather than electromechanically. An EFIS normally consists of a primary flight ...
(EFIS). All four engines were removed. Two of them were overhauled and reinstalled on the aircraft, while the other two were completely replaced by different JT3D-7 engines from ABX Air. Hush kits were installed on all of the engines for noise reduction. The aircraft's stall warning system was tested and declared functional.


Crew

Rather than a captain, a first officer and a flight engineer, Flight 827 was crewed by two captains (one flying, one monitoring), and a flight engineer. There were also three aircraft technicians on board. The captain who was the pilot monitoring (though acting as
pilot in command The pilot in command (PIC) of an aircraft is the person aboard an aircraft who is ultimately responsible for its operation and safety during flight. This would be the captain in a typical two- or three- pilot aircrew, or "pilot" if there is only ...
(PIC)) was 48-year-old Garth Avery, who had worked for Airborne Express since 1988 and had 8,087 flight hours, including 869 hours on the DC-8. He was seated in the right seat. Avery was also the airline's Boeing 767 flight manager as well as a flight instructor. The captain who was the pilot flying (though acting as a co-pilot) was 37-year-old William "Keith" Leming, who had worked for Airborne Express since 1991 and had logged 8,426 flight hours, with 1,509 of them on the DC-8. He was seated in the left seat. Leming was the manager of Airborne Express' DC-8 flight standards (the position previously having been held by Captain Avery) and had previously been a pilot for
Trans World Airlines Trans World Airlines (TWA) was a major airline in the United States that operated from 1930 until it was acquired by American Airlines in 2001. It was formed as Transcontinental & Western Air to operate a route from New York City to Los Angeles ...
. The flight engineer was 52-year-old Terry Waelti who, like Captain Avery, had been with Airborne Express since 1988. Waelti had 7,928 flight hours, including 2,576 hours on the DC-8. He was also a DC-8 examiner designated by the
Federal Aviation Administration The Federal Aviation Administration (FAA) is a Federal government of the United States, U.S. federal government agency within the United States Department of Transportation, U.S. Department of Transportation that regulates civil aviation in t ...
(FAA). Waelti had previously served in the
United States Air Force The United States Air Force (USAF) is the Air force, air service branch of the United States Department of Defense. It is one of the six United States Armed Forces and one of the eight uniformed services of the United States. Tracing its ori ...
(USAF) and was one of the USAF's first flight engineers to be qualified on the Boeing E-4B. The three technicians were 48-year-old Edward Bruce Goettsch, 39-year-old Kenneth Athey, and 36-year-old Brian C. Scully. Goettsch and Athey both worked for Airborne Express, while Scully worked for TIMCO.


Accident

Initially, Flight 827 had been scheduled to depart from
Piedmont Triad International Airport Piedmont Triad International Airport (; commonly referred to locally as "PTI") is an airport located in unincorporated Guilford County, North Carolina, west of Greensboro, serving the Piedmont Triad region of Greensboro, High Point and Winsto ...
on December 16, but was delayed due to maintenance. An attempt on December 21, (operated by the same crew) was cut short due to a hydraulic problem. Flight 827 finally departed at 17:40
Eastern Standard Time The Eastern Time Zone (ET) is a time zone encompassing part or all of 23 states in the eastern part of the United States, parts of eastern Canada, and the state of Quintana Roo in Mexico. * Eastern Standard Time (EST) is five hours behind ...
(EST) at nighttime on December 22, 1996, after being delayed due to additional maintenance. The flight climbed to and then to . Flight 827 was operating under instrument flight rules (IFR). After departing Greensboro, the aircraft was to fly northwest over New River Valley Airport's VOR, in
Pulaski County, Virginia Pulaski County is a county located in the southwestern part of the U.S. state of Virginia. As of the 2020 census, the population was 33,800. Its county seat is Pulaski. Pulaski County is part of the Blacksburg-Christiansburg metropolitan a ...
, then to
Beckley, West Virginia Beckley is a city in Raleigh County, West Virginia, United States, and its county seat. The population was 17,286 at the 2020 United States census, 2020 census, making it the List of municipalities in West Virginia, ninth-most populous city in th ...
, followed by other way points in Kentucky and Virginia, and then return to Greensboro. The flight was expected to last two hours. Shortly after reaching , the aircraft experienced
atmospheric icing Atmospheric icing occurs in the atmosphere when water droplets suspended in air freeze on objects they come in contact with. It is not the same as freezing rain, which is caused directly by precipitation. Atmospheric icing occurs on aircraft, ...
, which was indicated when the cockpit voice recorder (CVR) recorded captain Lemming saying, "we're gettin' a little bit of ice here," and "probably get out of this," at 17:48:34 and 17:48:37 respectively. Several landing gear, hydraulic, and engine tests were performed without incident. At 18:05, flight engineer Waelti said, "next thing is our stall series." The next item was a clean stall maneuver test. The crew would slow the aircraft down until the
stick shaker Stick, sticks or the stick may refer to: Thin elongated objects * Twig or branch * Walking stick, a device to facilitate balancing while walking * Shepherd's crook * Shillelagh * Swagger stick * Digging stick * Swizzle stick, used to stir drinks ...
activated, record the stall speed and that of the stick shaker activation, and then recover control of the aircraft. In other words, the flight crew would deliberately stall the aircraft. Captain Avery stated that the crew would stop trimming the aircraft at and that the stall speed (VS) was . Flight engineer Waelti stated that the stick shaker would activate at , which was higher than the calculated stall speed. The flight crew began gradually slowing the aircraft down by per second. At 18:07, engine power was increased. One minute later at 18:08, a buffeting sensation was experienced at . The following was recorded on the CVR: At this time, according to the flight data recorder (FDR), the aircraft was at . However, the stick shaker had failed to activate. The speed then decreased to and the aircraft entered a real stall. At 18:08:13, captain Lemming decided to terminate the test, called "set max power," and applied full engine power in an attempt to recover from the stall. Although all four engines started to accelerate, engine no. 2 accelerated more slowly. This engine subsequently experienced a compressor stall. Ground witnesses also noted that the aircraft was making "skipping or missing" sounds. At 18:09, Air Traffic Control (ATC) asked the flight if they had initiated an emergency descent, with captain Avery replying, "yes sir." This was the last communication (and only distress call) from Flight 827. At 18:09:35, the
ground proximity warning system A Ground Proximity Warning System (GPWS) is a system designed to alert pilots if their aircraft is in immediate danger of flying into the ground or an obstacle. The United States Federal Aviation Administration (FAA) defines GPWS as a type of ...
(GPWS) activated and sounded "terrain terrain, whoop whoop pull up." Three seconds later at 18:09:38, the aircraft crashed into a mountain travelling over in a nose-down wings-down position of 26 and 52 degrees, respectively. The crash site elevation was
mean sea level A mean is a quantity representing the "center" of a collection of numbers and is intermediate to the extreme values of the set of numbers. There are several kinds of means (or "measures of central tendency") in mathematics, especially in statist ...
(MSL). The aircraft exploded on impact. All six people on board were killed and the aircraft was destroyed.


Investigation

The
National Transportation Safety Board The National Transportation Safety Board (NTSB) is an independent U.S. government investigative agency responsible for civil transportation accident investigation. In this role, the NTSB investigates and reports on aviation accidents and inci ...
(NTSB) launched an investigation into the accident and arrived at the crash site the same day. Both flight recorders were recovered the next morning. Rescue teams also recovered all six bodies. Efforts to reach the accident site were initially hampered due to its remote location. The aircraft's flight controls were destroyed in the crash, but the NTSB recovered two trim jackscrews from the horizontal stabilizer. The NTSB recreated the stall in a simulator. In the simulation, the stick shaker activated at . Despite deepening the stall, no unexpected nose-down pitches or lateral rolls occurred in the simulator. The decreasing airspeed caused the nose to pitch up. In 1991, another Airborne Express DC-8 had entered a real stall during an FEF, but the flight crew was able to recover and test continued with no further incidents. In the 1991 incident, the stick-shaker activated the same time the buffeting sensation occurred. The Federal Aviation Administration (FAA) issued a revised stall recovery procedure to Airborne Express, which they agreed to incorporate. However, the airline had only partially incorporated the procedure at the time of the Flight 827 accident. Airborne Express' flight operation manual contained only a short section labeled "Test Flights" and the requirements for FEF's read: At the time of the accident, there were scattered showers of light rain and the cloud ceiling was between and . The reported surface weather at Mercer County Airport in Bluefield stated that visibility was two miles. Because of the aircraft experiencing icing, it experienced a buffet before the stall speed. The FDR indicated that the aircraft had entered a real stall at , four knots before the stall speed. The NTSB concluding that the icing, regardless of amount, (along with flight control rigging) did not contribute to the accident. Despite Captain Lemming's timely decision to terminate the stall test, he subsequently pulled back on the control column from five to ten degrees, allowing the aircraft to enter a real stall. The NTSB notes that he likely did this in an attempt to establish an appropriate pitch attitude and power setting. Captain Avery did not notice the incorrect flight control inputs made by captain Lemming, though he did attempt to instruct Lemming on to recover the airplane from the roll, but not how to recover from the stall. In addition he did not enhance his instructions or take over control of the aircraft himself. The NTSB noted that since both pilots were captains, had manager positions at the airline, and had similar backgrounds, they would have difficulty challenging each other because of a lack of command authority. Captain Avery, as PIC, should have monitored and challenged captain Lemming's actions, but both his PIC and instructional roles were informal on the accident flight. According to both flight recorders and the recovered horizontal stabilizer trim jackscrew, captain Lemming had trimmed the aircraft's horizontal stabilizer at instead of the intended . Airborne Express' procedures required the aircraft to be trimmed before the stall speed. Despite the incorrect trim setting, the aircraft would still have been recoverable from the stall. The NTSB concluded that the captain Lemming's incorrect trimming of the horizontal stabilizer was not a factor in the accident. The NTSB examined N827AX's maintenance records and reviewed Airborne Express' procedures for testing the stall warning system, but could not determine why the stick shaker was inoperative during the accident flight. In addition, the flight crew's situational awareness that the aircraft was in a stall was short, as they were distracted by the compressor stall on the no. 2 engine and communications with ATC. The NTSB also stated that an angle of attack display on the flight deck could have helped the crew situational awareness. The fact that the crew lacked a visual horizon at nighttime was another factor due to the aircraft being in instrument meteorological conditions (IMC) from the time the stall maneuver was performed until impact. Neither captain Avery nor captain Lemming had ever flown a DC-8 post modification on an FEF until December 21 (the initial FEF that was aborted), though the director of flight technical programs authorized Avery to serve as a pilot in command on post modification FEF's.


Final report

The NTSB released the final report on July 15, 1997. The "probable cause" section stated the following: The accident had been caused by pilot error due to captain Lemming's improper flight control inputs and captain Avery's failure to notice them. Another cause was Airborne Express failing to set up a proper program for FEFs, resulting in inadequate training. Contributing factors included the stick shaker being inoperative, inaccuracies in Airborne Express' flight simulators when simulating a stall, the compressor stall on the no. 2 engine which distracted the flight crew, the accident occurring at night (which resulted in the flight crew's lack of a visual horizon and other exterior cues), and Airborne Express not requiring flight tests to be completed before nightfall. Airborne Express agreed with the NTSB that the pilots used incorrect procedures, but disputed two other findings, citing that Avery did have prior experience controlling a DC-8 during a stall, and stated that the revised stall procedures were fully implemented at the time of the accident.


Aftermath

The NTSB issued seven safety recommendations to the FAA. The NTSB also reiterated a previous recommendation regarding the angle of attack following the crash of
American Airlines Flight 965 American Airlines Flight 965 was a regularly scheduled flight from Miami International Airport in Miami, Florida, to Alfonso Bonilla Aragón International Airport in Cali, Colombia. On December 20, 1995, the Boeing 757-200 flying this route ...
on December 20, 1995: Lynn Scully, the wife of Brian Scully, filed a lawsuit against Airborne Express for $20 million. Brian Scully's sister, Maureen DeMarco, was killed in the crash of
Comair Flight 3272 Comair Flight 3272 was a scheduled domestic passenger flight operated by Comair (United States), Comair from Cincinnati/Northern Kentucky International Airport, Cincinnati International Airport in Kentucky to Detroit Metropolitan Airport in Mic ...
on January 9, 1997. Maureen was headed to Brian's funeral.


Dramatization

This accident was featured in
season 25 A season is a division of the year based on changes in weather, ecology, and the number of daylight hours in a given region. On Earth, seasons are the result of the axial parallelism of Earth's axial tilt, tilted orbit around the Sun. In temperat ...
of
Mayday Mayday is an emergency procedure word used internationally as a distress signal in voice-procedure radio communications. It is used to signal a life-threatening emergency primarily by aviators and mariners, but in some countries local organiz ...
, titled "Fatal Test Flight".


See also

*
Air France Flight 447 Air France Flight 447 was a scheduled international passenger flight from Rio de Janeiro/Galeão International Airport, Rio de Janeiro, Brazil, to Charles de Gaulle Airport, Paris, France. On 1 June 2009, inconsistent airspeed indications and mi ...
*
Air Transport International Flight 782 Air Transport International Flight 782 was a ferry flight from Kansas City International Airport in Missouri to Westover Metropolitan Airport in Springfield, Massachusetts using a Douglas DC-8-63 with one of its 4 engines inoperative. On Februar ...
, another non-scheduled DC-8 flight that crashed one year previously *
Colgan Air Flight 3407 Colgan Air Flight 3407 was a scheduled passenger flight from Newark, New Jersey, to Buffalo, New York, on February 12, 2009. Approaching Buffalo, the aircraft, a Bombardier Q400, entered an aerodynamic stall from which it did not recover and ...
*
West Caribbean Airways Flight 708 West Caribbean Airways Flight 708 was a charter flight that crashed in northwest Venezuela in the early hours of 16 August 2005, killing all 160 passengers and crew on board. The plane, a McDonnell Douglas MD-80, McDonnell Douglas MD-82, registra ...
*
XL Airways Germany Flight 888T XL Airways Germany Flight 888T (GXL888T) was an acceptance flight for an Airbus A320 on 27 November 2008. The aircraft crashed into the Mediterranean Sea, off Canet-en-Roussillon on the French coast, close to the Spanish border, killing all se ...
, another flight test where the aircraft stalled and crashed * LAC Colombia Flight 028


Notes


References


External links


Cockpit voice recorder transcript and accident summary
{{Aviation accidents and incidents in the United States in the 1990s Aviation accidents and incidents in the United States in 1996 Airliner accidents and incidents in Virginia Airliner accidents and incidents caused by pilot error Accidents and incidents involving the Douglas DC-8 1996 in Virginia December 1996 in the United States Airliner accidents and incidents caused by instrument failure Airliner accidents and incidents caused by stalls