Ranger 1 was a prototype spacecraft launched as part of the
Ranger program
The Ranger program was a series of uncrewed space missions by the United States in the 1960s whose objective was to obtain the first close-up images of the surface of the Moon. The Ranger spacecraft were designed to take images of the lunar su ...
of
uncrewed space missions. Its primary mission was to test the performance of those functions and parts necessary for carrying out subsequent lunar and planetary missions; a secondary objective was to study the nature of particles and fields in the space environment. Due to a launch vehicle malfunction, the spacecraft could reach only
Low Earth orbit
A low Earth orbit (LEO) is an geocentric orbit, orbit around Earth with a orbital period, period of 128 minutes or less (making at least 11.25 orbits per day) and an orbital eccentricity, eccentricity less than 0.25. Most of the artificial object ...
, rather than the
high Earth orbit that had been planned, and was only able to complete part of its mission.
[ National Space Science Data Center, Ranger 1, NSSDC ID: 1961-021A]
Spacecraft design
The spacecraft was of the Ranger Block I design and consisted of a hexagonal base across upon which was mounted a cone-shaped high tower of aluminum struts and braces. Two solar panel wings measuring from tip to tip extended from the base. A high-gain directional dish antenna was attached to the bottom of the base. Spacecraft experiments and other equipment were mounted on the base and tower. Instruments aboard the spacecraft included a Lyman-alpha telescope, a
rubidium-vapor magnetometer, electrostatic analyzers, medium-energy range particle detectors, two triple coincidence telescopes, a cosmic-ray integrating
ionization chamber
The ionization chamber is the simplest type of gaseous ionisation detector, and is widely used for the detection and measurement of many types of ionizing radiation, including X-rays, gamma rays, alpha particles and beta particles. Conventionall ...
, cosmic dust detectors, and solar X-ray
scintillation counter
A scintillation counter is an instrument for detecting and measuring ionizing radiation by using the Electron excitation, excitation effect of incident radiation on a Scintillation (physics), scintillating material, and detecting the resultant li ...
s. There was no camera or midcourse correction engine on the Block I spacecraft.
The communications system included the high-gain antenna and an omnidirectional medium-gain antenna and two transmitters, one at 960.1
MHz
The hertz (symbol: Hz) is the unit of frequency in the International System of Units (SI), often described as being equivalent to one event (or cycle) per second. The hertz is an SI derived unit whose formal expression in terms of SI base u ...
with 0.25
watt
The watt (symbol: W) is the unit of Power (physics), power or radiant flux in the International System of Units (SI), equal to 1 joule per second or 1 kg⋅m2⋅s−3. It is used to quantification (science), quantify the rate of Work ...
s power output and the other at 960.05 MHz with 3 watts power output. Power was to be furnished by 8680 solar cells on the two panels, a silver-zinc battery, and smaller batteries on some of the experiments. Attitude control was provided by a solid-state timing controller,
Sun and
Earth
Earth is the third planet from the Sun and the only astronomical object known to Planetary habitability, harbor life. This is enabled by Earth being an ocean world, the only one in the Solar System sustaining liquid surface water. Almost all ...
sensors, and pitch and roll jets. The temperature was controlled passively by gold plating, white paint, and polished aluminum surfaces.
Mission
The Ranger 1 spacecraft was designed to go into an Earth
parking orbit and then move into a Earth orbit. The purpose of the mission was mainly as an engineering test to verify the functionality of the Ranger hardware.
Launch delays
* Delay of the 1st countdown
** July 26: Trajectory information required by the Range Safety Officer was delayed.
** July 27: A guidance system malfunction in the Atlas booster.
** July 28: Engineers found that the guidance program to be fed into the Cape computer contained an error.
* 1st countdown. July 29.
** 83 minutes before launch: Power interruptions occurred, requiring momentary holds to permit all stations to check and recover.
** 28 minutes before launch: Commercial electrical power failed. Inadequate allowance had been made for changes in cable sag caused by variations in temperature on the new power poles recently installed at
Cape Canaveral Air Force Station
Cape Canaveral Space Force Station (CCSFS) is an installation of the United States Space Force's Space Launch Delta 45, located on Cape Canaveral in Brevard County, Florida.
Headquartered at the nearby Patrick Space Force Base, the sta ...
.
* 2nd countdown. July 30. Engineers discovered a leak in Ranger's attitude control gas system.
* 3rd countdown. July 31. A LOX tank pressure regulator seal developed a leak due to damage resulting from improper handling.
* 4th countdown. August 1. Ground controllers turned on a spacecraft command applying high voltage to the scientific experiments for calibration purposes. Immediately all stations reported a major spacecraft failure. An electrical malfunction had triggered multiple commands from the central clock timer, and Ranger 1 "turned on" as it had been programmed to do in orbit. The explosive squibs fired, solar panels extended inside the shroud, and all the experiments commenced to operate. Project engineers disengaged Ranger 1 from the Agena and hastily returned it to Hangar AE. Meantime, the launch was rescheduled for August 22, the next available opportunity. Subsequent tests and investigations determined the activating mechanism to have been a voltage discharge to the spacecraft frame; although engineers suspected one or two of the scientific instruments, they could not determine the precise source of the discharge with certainty. In the days that followed, they replaced and requalified the damaged parts and modified the circuitry to prevent a recurrence of this kind of failure.
[ LUNAR IMPACT: A History of Project Ranger - Part I]
Launch
During the first half of 1961, Lockheed introduced the new Agena B stage which replaced the early test-model Agena A of 1959-60. Agena B was more powerful and had in-orbit restart capability. Its first flight with the launch of
Midas 3 on July 24 was successful. Several frustrating delays in Ranger 1's launch occurred, including one episode where the spacecraft's timer inadvertently activated on the pad, causing the solar panels to be deployed inside the payload shroud. After removing Ranger 1 and repairing it, the launch was carried out at 6:04 AM EST on August 23. All went well up to orbital injection, but the planned Agena restart went awry when the engine shut down after only a few seconds, putting the probe in a 312x105 mile track. Subsequent investigation concluded that an electrical circuit in the Agena had overheated from exposure to the Sun. The unintended orbit made it difficult to operate Ranger 1's systems correctly, although ground controllers tried to work around it. The main problem they faced was with the solar panels; Ranger 1 would experience 90 minutes of darkness while passing around the nighttime side of the Earth. In addition, the antennas at NASA's various tracking stations had difficulty locking onto the probe due to its orbital plane. During this time, the computer system repeatedly fired the attitude control jets in a vain attempt to lock onto the Sun with the effect that only one day after launch, the probe ran out of attitude control gas. At this point, it could not be stabilized and the solar panels lost their lock on the Sun. Ranger 1 thus reverted to battery power and continued transmitting until the batteries ran down on August 27 and all signals from the probe ceased. It was not a total loss; the spacecraft systems had worked well and some data on cosmic rays and radiation was returned, however the low orbit precluded the use of the
magnetometer. After four days and 111 orbits, Ranger 1 reentered and burned up over the
Gulf of Mexico
The Gulf of Mexico () is an oceanic basin and a marginal sea of the Atlantic Ocean, mostly surrounded by the North American continent. It is bounded on the northeast, north, and northwest by the Gulf Coast of the United States; on the southw ...
.
Footnotes
See also
*
Ranger program
The Ranger program was a series of uncrewed space missions by the United States in the 1960s whose objective was to obtain the first close-up images of the surface of the Moon. The Ranger spacecraft were designed to take images of the lunar su ...
*
Timeline of Solar System exploration
*
List of artificial objects on the Moon
This is a partial list of artificial materials left on the Moon, many during the missions of the Apollo program. The table below does not include lesser Apollo mission artificial objects, such as a hammer and other tools, Laser Ranging Retroflect ...
References
*
*
External links
Space flight operations memorandum - Ranger 1 (Post-Flight Mission Analysis)Lunar impact: A history of Project Ranger (PDF) 1977
{{Orbital launches in 1961
1
Spacecraft launched in 1961
Spacecraft which reentered in 1961